Adjusted probing depth for TAZ.

- Testing in the cluster revealed that the probing was going too deep
  before giving up and rewiping, which could lead to the head making
  contact late and causing a print with an unlevel bed. Adjusted values
  so they match prior FW (and not probing as deeply).
- Probe depth for Mini also adjusted to match Gladiola FW.
master
Marcio Teixeira 7 years ago
parent 6766c273cc
commit fb159a65e7

@ -13,7 +13,7 @@
* got disabled.
*/
#define LULZBOT_FW_VERSION ".16" // Change this with each update
#define LULZBOT_FW_VERSION ".17" // Change this with each update
#if ( \
!defined(LULZBOT_Gladiola_Mini) && \
@ -253,7 +253,7 @@
#define LULZBOT_Z_SAFE_HOMING_Y_POINT (258)
#define LULZBOT_Z_HOMING_HEIGHT 5
#define LULZBOT_AFTER_Z_HOME_Z_RAISE 5
#define LULZBOT_AFTER_Z_HOME_Z_RAISE 10
#define LULZBOT_AFTER_Z_HOME_Z_ORIGIN 0
#elif defined(LULZBOT_Juniper_TAZ5)
// Set safe homing position so fan duct does not hit.
@ -959,7 +959,11 @@
/*************************** REWIPE FUNCTIONALITY *******************************/
#define LULZBOT_NUM_REWIPES 1
#define LULZBOT_BED_PROBE_MIN -3 // Limit on pushing into the bed
#if defined(LULZBOT_IS_TAZ)
#define LULZBOT_BED_PROBE_MIN 0 // Limit on pushing into the bed
#else
#define LULZBOT_BED_PROBE_MIN -4 // Limit on pushing into the bed
#endif
#define LULZBOT_PROBE_Z_WITH_REWIPE(speed) \
/* do_probe_move returns true when it fails to hit an endstop, meaning we need to rewipe */ \

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